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Introduction Background
Incident Description
Lessons Learned
Management of Process Safety
Safety Equipment

CSB Safety Bulletins offer advisory information on good practices for managing chemical process hazards. Actual CSB case histories provide supporting information. Safety Bulletins differ from CSB Investigation Reports in that they do not comprehensively review all the causes of an incident.


U.S. Chemical Safety and Hazard Investigation Board
Office of Investigations and Safety Programs
2175 K Street NW, Suite 400
Washington, DC 20037
202-261-7600
http://www.chemsafety.gov




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Incident Description . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 
Pre-Incident Activity—
A severe storm on November 24 caused an electric power outage in the refinery. The storm interrupted process operations and also stopped the production of steam. At the delayed coking unit, the on-line drum had been filling for about an hour and was approximately 7 percent full. The other drum was full and was being cooled.

Although electric power was restored after 2 hours, an additional 10 hours passed before steam production was re-established. During the interim, the tarry oil in the piping between the furnace and the partially filled drum cooled and started to solidify. Once steam was restored, the operators were unsuccessful in attempting to inject it into the drum through the normal route because of the plugged piping. (When normally injected, steam creates passages in the tarry mass through which cooling water can later flow. It also drives off remaining residual volatile petroleum and sulfur compounds from the coke.)

A process interruption in 1996 had also resulted in a partially filled drum. At that time, water was injected into the drum to cool the material inside. However, when the drum was opened, a torrent of water, heavy oil, and coke spewed out—which created a hazard and required a major cleanup. An internal investigation team recommended that procedures be written for cooling/emptying partially filled drums. However, this task was not completed.

On the day of the fire, neither the process supervisor nor the operators had any written procedures for handling partially filled drums. The process supervisor was aware of the seriousness of the previous incident. He left instructions directing the night shift not to add any water, and instead to allow the drum and its contents to simply stand and cool overnight. On the following morning, he met with the operators to determine how to empty the partially filled drum. No engineers, who could have provided technical support, were present at this meeting.

Preliminary Operations
The supervisor and operators observed that the exposed part of the bottom flange of the drum felt cool to the touch. They also noted that temperature-sensing devices located beneath the insulation on the outside surface of the drum indicated approximately 230 degrees Fahrenheit (°F), as compared to the 800°F of a typically full drum.

One operator suggested adding 100 barrels of water to the drum. However, the supervisor was concerned about such a course of action because of the previous incident. Upon further discussion, they decided—because part of the drum felt cool, and the temperature-sensing devices read only 230ºF—that it was not very hot inside and it was safe to open the vessel as long as they first injected some steam.

An operator connected a steam hose to the oil inlet piping at the bottom of the drum. Several witnesses said that the steam warmed the top of the piping, but the bottom remained cool. It is likely that steam flow had been established, but the rate of flow was low.

Opening the Vessel
Personnel expected a tarry mass to drain from the drum. The supervisor and process operator directed that the drum be opened with a minimum number of people present. Because they were also concerned that the limited flow of steam might not sufficiently strip all the toxic compounds from the tar inside the vessel, they required that the workers removing the bolts on the drum heads wear self-contained breathing apparatus. The top head was unbolted and lifted from the drum. The bottom head was also unbolted and held in place by a hydraulic dolly. The operator then activated a release mechanism to lower the dolly. Witnesses reported hearing a whooshing sound and seeing a white cloud of vapor emanate from the bottom of the drum. The hot petroleum vapor burst into flames. The process supervisor, an operator, and the four contract personnel assisting were caught in the fire and did not survive (Figure 2).

After the incident, Equilon relocated the controls for the hydraulic dolly to allow workers to position themselves farther from a drum when opening it.

Followup Analysis
The supervisor and operators analyzed the situation and devised process changes to empty the drum. The relative coolness of the bottom flange erroneously suggested to them that the temperature inside the drum was also cool—when, in fact, only the material adjacent to the inside walls had cooled. Unknown to the coker unit personnel present, the core of the mass remained insulated from heat loss. Within the core, residual heat continued to break down the petroleum, creating a pocket of hot pressurized volatile oil. Had the limitations of temperature-sensing devices been better understood, personnel may have realized that the low temperature readings were not representative of the hot core. It was assumed that the entire drum contents had cooled to safe levels during the 2 days since the power failure. However, heat transfer calculations would have indicated that weeks would be required for the drum contents to cool sufficiently via heat losses to the ambient environment.
 

Fire control efforts
at Equilon refinery
Matt Wells, Skagit Valley Herald

 

 

 


The relative coolness of the bottom flange erroneously suggested that the temperature inside the drum was also cool—
when, in fact, only the material adjacent to the inside walls had cooled.

 

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